Home

Tuesday, April 6, 2021

Pioneer SX-880 Receiver Restoration

Unit: AM/FM Stereo Receiver
Manufacturer: Pioneer
Model: SX-880
SN: YE3607162S

Today I'm showcasing a Pioneer SX-880 receiver that came in for restoration. The SX-880 is a big brother of Pioneer SX-780 which I restored about a year ago. It produces 60 watts per channel into 8 ohms with no more than 0.05% total harmonic distortion. It was manufactured from 1978 through 1979. The list price in 1978 was $425.00. According to the Pioneer database, this unit was manufactured in May 1978.

Pioneer SX-880_After restoration

Initial Evaluation and Cleaning

This particular unit came in with several problems and most of them were related to the dirty and/or oxidized switches and pots. The sound from both channels was very distorted and intermittent. Occasionally one channel cuts out the sound completely. The initial evaluation showed that the contacts in all three switches (TAPE MONITOR, TAPE DUPLICATE, and MODE) are severely oxidized due to age. The BALANCE and VOLUME pots were dirty as well. All other switches and pots were in good shape. So, I decided to start the restoration from a good cleaning of all switches and pots to see if there are any other issues related to the sound in this unit.

First of all, I carefully vacuumed this unit inside and cleaned all boards as much as possible from the dust. It is always worth cleaning any vintage gear before servicing. Dust can carry a static charge and short-circuit the electronics. That's why all PCBs should be kept clean from dust as much as possible.

Tuner board - before and after cleaning

Pioneer SX-880_Tuner Board_before cleaning

Pioneer SX-880_Tuner Board_after cleaning

Variable capacitor - before and after cleaning

Pioneer SX-880_Variable Capacitor_before cleaning

Pioneer SX-880_Variable Capacitor_after cleaning

Transformer & Filter capacitors - before and after cleaning

Pioneer SX-880_Transformer & Filter Capacitors_before cleaning

Pioneer SX-880_Transformer & Filter Capacitors_after cleaning

To clean the pots and switches in SX-880 the wooden cover should be removed. However, all potentiometers might be much easier to clean if both the front panel and large mounting plate are also removed. In addition, it will provide excellent access to all electronic components located close to the mounting plate.

Black mounting plate removed - much easier to clean all pots and switches, and replace all e-caps

Pioneer SX-880_Black mounting plate removed_01

Pioneer SX-880_Black mounting plate removed_02

Pioneer SX-880_Black mounting plate removed_03

I thoroughly cleaned all pots and switches with DeoxIT 5% contact cleaner and lubricated them with DeoxIT FaderLube 5% spray. A quick test showed that a clear sound was restored from both channels.

AF Amplifier Board GWK-119

The next issue was related to three transistors Q26, Q27 and Q30 installed in the power supply circuit. These transistors are running very hot under normal operating conditions. The original heat sink attached to each transistor is rather small to efficiently dissipate the heat. As a result, a PCB discoloration is often observed around those transistors. In extreme cases the PCB around transistor Q26 could be severely damaged and the solder joint cracks can often be detected. It results in intermittent contact problems. I decided to retire those three transistors and replace them with modern Fairchild transistors. Two NPN transistors Q26 and Q30 were replaced with KSC2073TU, and one PNP transistor Q27 was replaced with KSA940TU. A new silicone thermal compound (Wakefield-Vette, 120 series) was applied between each transistor and the heat sink.

PCB discoloration around transistor Q26

Pioneer SX-880_PCB discoloration around Q26

Original transistors Q26, Q27, and Q30 from the power supply were replaced with modern Fairchild transistors

Pioneer SX-880_Original and new transistors Q26, Q27 and Q30

The power supply circuit has ten electrolytic capacitors: C407 thru C410, C413, C414, and C420 thru C423. All of them were replaced with low impedance and high-reliability Nichicon UPW/UPM caps. Those e-caps are designed for switching power supplies and can operate in the temperature range from -55 to +105 C. The original e-caps installed in vintage gears from the 70's have a maximum operating temperature of +85C. 

I found an error in the schematic concerning the e-cap C410. The schematic shows this capacitor as 100uF/16V despite the original capacitor installed on the board being 220uF/16V. Most probably this is just due to design improvements not well documented by Pioneer. I replaced this e-cap with a Nichicon UPW capacitor, 220uF/25V.

All original e-caps were tested with Atlas ESR70 capacitance meter and results are below. Most of them are still within the factory capacitance tolerance. However, the modern low impedance Nichicon capacitors have lower ESR and more tight spec on capacitance tolerance.

Test results on original capacitors removed from the power supply circuit:

C407: rated capacitance – 470uF, measured – 289uF, ESR – 0.06Ω, deviation: -39%
C408: rated capacitance – 330uF, measured – 320uF, ESR – 0.06Ω, deviation: +3%
C409: rated capacitance – 100uF, measured – 99uF, ESR – 0.23Ω, deviation: -1%
C410: rated capacitance – 220uF, measured – 139uF, ESR – 0.33Ω, deviation: -37%
C413: rated capacitance – 3.3uF, measured – 4.1uF, ESR – 1.55Ω, deviation: +24%
C414: rated capacitance – 3.3uF, measured – 4.2uF, ESR – 1.11Ω, deviation: +27%
C420: rated capacitance – 47uF, measured – 38uF, ESR – 0.26Ω, deviation: -19%
C421: rated capacitance – 47uF, measured – 37uF, ESR – 0.36Ω, deviation: -21%
C422: rated capacitance – 100uF, measured – 119uF, ESR – 0.14Ω, deviation: +19%
C423: rated capacitance – 100uF, measured – 97uF, ESR – 0.18Ω, deviation: -3%

The protection circuit has five electrolytic capacitors: C415 thru C419. Two of them (C415 and C416) are solid tantalum capacitors. I replaced these e-caps with high-quality film polyester Kemet caps. The remaining e-caps were replaced with Nichicon UPW caps.

The FM muting circuit has five electrolytic capacitors: C301 thru C305. Two of them C302 and C303 are low leakage e-caps. I replaced C302/C303 and C304/C305 with film polyester WIMA MKS2 caps. The remaining capacitor C301 was replaced with a low impedance Nichicon UPW cap.

The phono amplifier circuit has eight electrolytic capacitors: C101/C102, C105/C106, C115/C116, and C119/C120. Four of them C101/C102 and C115/C116 are low leakage capacitors installed in the signal path. I replaced them with modern low leakage Nichicon UKL caps. The other four aluminum e-caps were replaced with low impedance Nichicon UPW caps. The Nichicon UKL caps have lower ESR which is beneficial for capacitors installed in the signal path of the circuit. For example, the original low leakage e-cap with capacitance 2.2uF/50V has the ESR in the range from 2.2 to 2.4Ω. The modern Nichicon UKL cap with the same capacitance of 2.2uF/50V has a typical ESR ranging from 1.0 to 1.2Ω.

Test results on original capacitors removed from the phono amplifier circuit:

C101: rated capacitance – 2.2uF, measured – 2.2uF, ESR – 2.2Ω, deviation: 0%
C102: rated capacitance – 2.2uF, measured – 2.2uF, ESR – 2.3Ω, deviation: 0%
C105: rated capacitance – 470uF, measured – 544uF, ESR – 0.18Ω, deviation: +16%
C106: rated capacitance – 470uF, measured – 560uF, ESR – 0.15Ω, deviation: +19%
C115: rated capacitance – 2.2uF, measured – 2.3uF, ESR – 2.2Ω, deviation: +5%
C116: rated capacitance – 2.2uF, measured – 2.2uF, ESR – 2.4Ω, deviation: 0%
C119: rated capacitance – 100uF, measured – 124uF, ESR – 0.18Ω, deviation: +24%
C120: rated capacitance – 100uF, measured – 131uF, ESR – 0.18Ω, deviation: +31%

The tone control circuit has twelve electrolytic capacitors: C205/C206, C209/C210, C215/C216, C217/C218, C227/C228, and C229/C230. All of them (except C209/C210 and C215/C216) are low leakage capacitors installed in the signal path. I replaced e-caps C205/C206 with film polyester WIMA MKS2 caps, C217/C218 and C227/C228 with low leakage Nichicon UKL caps, and C229/C230 with film polyester Kemet caps. 

Ideally, all electrolytic capacitors installed in the signal path should be replaced with high-quality film capacitors. However, the size of modern film capacitors with capacitance 2.2uF and higher is rather large and does not always fit the position of the original e-cap. Therefore, I usually replace all capacitors with capacitance 1uF and lower with high-quality film polyester capacitors (WIMA or Kemet). The modern film polyester capacitors have excellent properties and zero ESR. All other capacitors with capacitance 2.2uF and higher installed in the signal path are usually replaced with low leakage Nichicon UKL caps.

Two pictures below show the measured capacitance and ESR of the original low leakage e-cap C205 (1uF/50V) and modern film polyester capacitor with the same rated capacitance and operating voltage. The original e-cap still holds the rated capacitance close to 1uF (the tolerance is just +15%) but its ESR is rather high - 5.1Ω. The modern WIMA film cap has zero ESR and a very tight spec on capacitance tolerance.

Original low leakage e-cap C205, 1uF/50V - the ESR is high

Pioneer SX-880_C205_Original LL e-cap

WIMA film polyester capacitor, 1uF/50V - the ESR is zero

Pioneer SX-880_C205_WIMA film cap

Several pictures below show the AF Amplifier board before and after service.

AF Amplifier Board - before servicing

Pioneer SX-880_AF Amplifier Board_before servicing_01

Pioneer SX-880_AF Amplifier Board_before servicing_02

Pioneer SX-880_AF Amplifier Board_before servicing_03

AF Amplifier Board - after servicing

Pioneer SX-880_AF Amplifier Board_after servicing_01

Pioneer SX-880_AF Amplifier Board_after servicing_02

Pioneer SX-880_AF Amplifier Board_after servicing_03

Pioneer SX-880_AF Amplifier Board_after servicing_04

Excellent access to all e-caps when the black mounting plate is removed - new caps installed

Pioneer SX-880_Black mounting plate removed_replaced e-caps_01

Pioneer SX-880_Black mounting plate removed_replaced e-caps_02

Pioneer SX-880_Black mounting plate removed_replaced e-caps_03

Meter Assembly Board GWX-193

The meter assembly board is mounted on the chassis with three plastic clips. The board is hard to service without removing it from the chassis. I carefully pulled off those three clips using two small flat screwdrivers. The plastic clips are very easy to break since they became rather brittle due to aging. So, take your time and work slowly if you need to need to service this board. It has only four electrolytic capacitors C501 thru C504 which were replaced with low impedance Nichicon UPW caps.

Meter assembly board - after servicing

Pioneer SX-880_C205_Meter Assembly Board_After servicing

Dial Lamps

The old dial bulbs in this unit were replaced with new incandescent lamps. To reflect the light and diffuse the heat coming from these bulbs I attached a strip of foil tape inside the top cover. It substantially reduces the heat coming from incandescent bulbs and protects the top cover and veneer from heat damage.

DC Balance and Idle Current Adjustments

The DC balance and idle current were adjusted according to the service manual. No dummy load or input signal is required for this adjustment. 

The DC balance is measured between pin 5 and ground on the left channel, and between pin 12 and ground on the right channel. It should be adjusted as close to zero volts as possible. The blue trimmers VR5 and VR6 are used for this adjustment on the left and right channel, respectively. I adjusted the DC balance to ~3mV on each channel.

The idle current (or strictly speaking the bias) is measured between pins 8 and 10 on the left channel, and between pins 14 and 16 on the right channel. This voltage was adjusted to ~32mV with trimmer VR7 (left channel) and VR8 (right channel), respectively.

DC balance on the left and right channel after restoration

Pioneer SX-880_DC balance_left channel_pin 5 and ground

Pioneer SX-880_DC balance_right channel_pin 12 and ground

Idle current (Bias) on the left and right channel after restoration

Pioneer SX-880_Idle current_left channel_pins 8 and 10

Pioneer SX-880_Idle current_right channel_pins 14 and 16

Power Meters Adjustment

An AC voltmeter and function generator are required to adjust power meters. A sine-wave signal of 1 kHz, 150mV should be applied to the AUX terminals. The level of this signal should be adjusted so that the voltage on the SPEAKERS terminals reads 21.9 VRMS. Then, the trimming resistors VR9 and VR10 should be adjusted so that the power meters read 60W.

As usual, all the knobs and the faceplate were gently cleaned in warm water with dish soap. I also slightly polished all knobs by Mothers Mag & Aluminum polish to remove some small spots of aluminum oxidation.

The final result can be seen in the photos below. Please watch a short demo video at the end of this post. Thank you for reading.

Pioneer SX-880 - after restoration

Pioneer SX-880_After restoration with replaced parts

Pioneer SX-880_After restoration_02

Pioneer SX-880_After restoration

Demo video after repair & restoration

Sunday, March 21, 2021

Onkyo TA-630D Cassette Deck Restoration

Unit: Stereo Cassette Tape Deck
Manufacturer: Onkyo
Model: TA-630D
SN: 10062943

I bought this cassette tape deck about two years ago from the original owner for just $25. The deck is in excellent cosmetic condition and there are only two almost invisible minor scratches on the faceplate. The owner told me that the last time he played the music on this deck was at least ten years ago. We met in a public place and I was not able to check whether it is working or not. But it was still a great deal since he wanted just $25 for it! I usually don't buy or restore vintage tape recorders because they often have problems with the transport mechanism, which I am not an expert in. But this tape deck was cheap, almost in perfect cosmetic condition, and most importantly for me, it has two large black VU meters! I am in love with vintage gears having VU meters. So, I bought it hoping to restore and keep it in my personal collection.

Onkyo TA-630D_After restoration_01

The Onkyo TA-630D is a stereo cassette deck with Dolby B noise reduction. It has 2 heads, belt-driven single-capstan transport, manual tape type selection handling normal, chrome and ferro-chrome tapes with additional manual equalization selection, and two large analog needle meters. The frequency response is from 30Hz to 18kHz on ferro-chrome tape and the signal to noise ratio is 68dB. It was manufactured from 1978 to 1980 with a list price of $350.

Belt Replacement

When I removed the top cover to check this unit inside I immediately noticed that we have a big problem here. The flat belt (Motor-Flywheel) and square-cut belt (Motor-pulley) have degraded so badly over time that both turned into sticky mush. Well, it looks like it wouldn't be an easy project. I checked online to get some guidance on how to replace these belts on this unit but with no success. There are just a few videos posted on YouTube about servicing Onkyo TA-630D but without good instructions for belt replacement. The service manual is also not very helpful for the belt replacement process. So, I decided to replace both belts based on my knowledge and experience with other cassette decks I restored before.

Further investigation revealed that this is definitely not a service-friendly cassette deck. I didn't find a way to replace two belts without disassembling and removing the metal bracket holding the motor and flywheel. Therefore, I initially removed the motor to clean its pulley from the sticky mush. This was an easy step but took some time to thoroughly clean the motor pulley from this messy stuff.

Sticky mush on the motor pulley from the old belt

Onkyo TA-630D_Sticky mush on motor pulley_01

Onkyo TA-630D_Sticky mush on motor pulley_02

Then, I tried to remove the sticky mush from the flywheel as much as possible before removing the metal bracket. I used a lot of Q-tips and isopropyl alcohol for that job.

Onkyo TA-630D_Sticky mush on flywheel

Eventually, I unscrew four small screws, removed the metal bracket, and pulled out the flywheel. I recommend paying attention to this step and taking a lot of pictures. Don't lose the poly washer and tension spring from the flywheel!

Metal bracket holding the motor and flywheel

Onkyo TA-630D_Metal bracket holding the motor and flywheel

Metal bracket and flywheel removed

Onkyo TA-630D_Metal bracket removed

I removed the residue of the old belt from all pulleys and cleaned them with isopropyl alcohol. The old lithium grease on most metal levers was mostly dried out. I removed this grease from all parts as much as I could and applied a new white lithium grease. The FF key on this unit was stuck but eventually came free with a little extra effort. I exercised all keys to make sure that the new grease penetrated between each lever and everything works smoothly.

The new flat belt (Motor-Flywheel) was installed in two steps. First of all, I installed a flywheel back and put a new flat belt on it. Then I installed the metal bracket trying not to damage a new flat belt and secured it with four screws. This step is the most critical one because the working space is really very limited here and a new belt tends to come off from the flywheel. So, take your time and don't rush at this step. When the metal bracket was successfully installed I mounted the motor on it and secured it with two screws. Then, using a pair of tweezers I was able to hang the belt to the motor pin.

A new flat belt (Motor-Flywheel) installed

Onkyo TA-630D_New flat motor belt installed

A new square cut belt (Motor-pulley) is fairly easy to install now since everything is mostly assembled. Double check the service manual to figure out how this belt should be installed. I used a pair of tweezers and with some patience was able to hang this belt as well.

A new square cut belt (Motor-pulley) installed

Onkyo TA-630D_New square cut belt installed

Onkyo TA-630D_New square cut belt installed_02

Cassette chassis assembled - back side

Onkyo TA-630D_Cassette chassis assembled

The last belt to replace is a counter belt. To access this belt one should remove the cassette door, cassette case, and cassette case plate. I didn't have any trouble removing these parts since the design is rather simple and it was intuitively clear what to do at each step.

Cassette door, case, and plate removed

Onkyo TA-630D_Cassette door, case and plate removed

Surprisingly but this belt survived and was still in pretty good condition. I vacuumed the deck chassis, cleaned the capstan, pinch roller, and both heads with isopropyl alcohol. Then applied a new white lithium grease to the rubbing metal parts and installed a new counter belt.

Clean chassis with new counter belt installed

Onkyo TA-630D_Clean chassis with new counter belt installed

For reference, I used the following belts in Onkyo TA-630D (Russell Industries, Inc. Cross-reference manual):
Flat belt (Motor-Flywheel) - FRZ7.5
Square cut belt (Motor-pulley) - SCQ8.2
Counter belt - SCY7.0

VU Meter Lamps

The lamp in the right channel VU meter has burned out and I decided to replace it with a new axial lamp. The meter is attached to the metal plate with double-sided tape. I used an X-ACTO #2 Knife to separate the meter from the metal plate. Pay attention to this step and don't apply too much force trying to separate it from the metal plate. Instead, try to carefully trim the double side tape with a proper knife/blade. The meter can be easily damaged due to extensive stress.

The lens is attached to the meter body with transparent tape which is not so easy to recognize at a first glance. I peeled off part of this transparent tape from the sides and carefully separated the lens from the meter body. According to the service manual, the original VU meter lamp is an axial 6.3V/100mA lamp. I replaced it with a new axial 6V/100mA lamp. The original lamp is a frosted bulb with a green tint whereas a new one is clear glass. I didn't find a suitable material to replicate the original green filter. The obvious option would be a green transparent tape wrapped around the lamp. But in that case, the tape would suffer from the extensive heat. So, I decided to leave it alone but also replace the original axial lamp from the left VU meter. At least both VU meters would match each other. Please leave a comment under this post if you have a better solution for a green filter.

VU Meters - the axial lamp in the right meter is burned out

Onkyo TA-630D_VU Meters_Original axial lamps

Each VU meter is attached to the metal plate with a double-sided tape

Onkyo TA-630D_VU Meters_Attached to the metal plate

Transparent tape on the sides of the VU meter lens

Onkyo TA-630D_VU Meters_Lens

Right VU meter - burned axial lamp

Onkyo TA-630D_Right VU Meter_Burned axial lamp

Right VU meter - new axial lamp installed

Onkyo TA-630D_Right VU Meter_New axial lamp

VU meters with new axial lamps

Onkyo TA-630D_New axial lamps in VU meters

I cleaned all the knobs and the faceplate in warm water with dish soap. All pots and switches have been cleaned with DeoxIT 5% contact cleaner and lubricated with DeoxIT FaderLube 5% spray.

The final result can be seen in the photos below. The transport mechanism is working properly again, all levers move smoothly and I am enjoying how it looks and plays music. Thank you for reading.

Onkyo TA-630D - after restoration

Onkyo TA-630D_After restoration_01

Onkyo TA-630D_After restoration_02